Central System Pigging
Pigging refers to the practice of using pipeline inspection gauges or "pigs" to clean the inner walls of a pipe while it is still in operation. Pigs get their name from the squealing sound they make while traveling through the pipeline.
Overview
The flow capacity of the central system has been declining for the past
15 years due to a build-up of calcium carbonate (CaCO2) on the inner wall of the pipe. Because of the increased friction, water levels in the pipe stands and the vent structures rise and overflow at high flows. The sections of the central system that have experienced the most problems are from the first pipe stand (Sta 2976+02.5) to pipe stand (Sta4049+96.88).
CRMWA’s aim has been to increase the flow in the central system back to
its original capacity or as close to it as possible. In 1994, CRMWA
began working in conjunction with Texas Tech University on a project to
remove the buildup of CaCO2 by injecting carbon dioxide
directly into the central system. This experimental project was
unsuccessful in removing a significant amount of the buildup inside the
pipe.
Planning for efforts to try to pig the central system began in early
1997. The purpose of this project was to determine if the pigging would
be effective in cleaning the pipe, therefore, only one or two sections
were budgeted to be pigged. If the pigging project was successful, then
other sections would be pigged at a later time.
Design & Planning
Choosing a Test Section
The first objective was to determine which section or sections of the
central system would serve as the best trial run for the pigging. Since
the project was experimental in determining if the pigging would be
effective or not, the aim was to find a section that would be the
simplest and the least expensive.
The most important feature of the system, when considering what section
to pig, proved to be the size of the outlet sump. Some of the pipe
stands have outlet sumps which are not as wide as the diameter of the
pipe. Since this would make launching more difficult and possibly
require a different kind of pig, these sections were not considered for
this initial project, though there are ongoing discussions with pig
manufactures to ensure that pigs can be made to accommodate these
sections.
One section (Pipe Stand 3374 + 98.7 to Pipe Stand 3617 + 00.67) has a
decrease in pipe diameter from 72 inches to 66 inches, which caused some
concern because of the additional uncertainties of a reduction in the
pipe diameter. This section was not chosen for this reason, especially
since this was an experimental project. Other sections were not chosen
for similar reasons. The section that appeared to present the least
amount of problems or unknowns was the 66-inch between Pipe Stands 3617
and 3776+97.93 just east of Happy, Texas. The outlet sump was large
enough to allow the pig to be lowered and positioned up to the pipe
opening.
Pig Design
There are many different kinds of pigs with different shapes and
materials of construction that serve a variety of pipe cleaning
functions. Initially, a swab pig (a foam pig without a polyurethane
coating) was recommended to act as a test pig since it is very flexible
and not likely to become lodged in the pipe. The use of a swab pig was
later abandoned since these pigs usually only help in determining if
valves are open in a complex pipe system and which route the pig will
take. These were not unknowns in our case and it was decided to use only
the cleaner pig.
The most important function for the cleaner pig (foam pig with
polyurethane coating and abrasive straps) was to remove the CaCO2
all together or smooth the buildup enough to provide increased capacity.
The recommendation from several pig manufacturers was to use wire brush
straps around the pig to act as the primary cleaning/scrubbing agent.
Samples of the wire brush straps were hand applied to the inner wall of
the pipe during an inspection in January 1998. The wire brush seemed to
be somewhat effective after several passes. Spencer Cubbage of Flowmore
Services, Inc. was present to assess the pipe and the project. His
recommendation was to use wire brushes and to run the pig at slow rate
(approximately 1.5 to 2.0 ft/sec). He also recommended the diameter of
the pig be equal to that of the pipe. Jim Gammill of Girard Industries,
Inc. recommended higher flow rates (3.0 to 5.0 ft/sec) and a pig
diameter of 1 inch greater than the pipe. Since Girard Industries, Inc.
submitted the low bid and was awarded the contract, their recommendation
was followed.
Launching the Pig
There were several potential problems when it came to launching the pig. The biggest problem was the fact that the pig would float and possibly have an upward buoyant force of 8,000 lbs. when submerged in water. If the pig could not be forced completely into the pipe, then something would have to hold the pig down as the water level rose. It was questionable that the pig could be forced into the pipe because of it being oversized. Also, water had to get by the pig to fill the partially drained line so that surging could be minimized. Several ideas were considered, but the simplest solution was to bolt steel pipe beams inside the sump over the top of the pig to hold it down as the pipe stand was being filled. Two pieces of pipe were welded together (in the shape of a fork) and put in front of the pig to prevent it from launching while the pipe was being filled. Figure 1 below is a photo of the pig being held in place with the pipe beams. Once the pipe was filled, the steel pipe would be removed and the pig could be launched.

Figure 1 - Pig in Sump of Pipe Stand
Pig Retrieval
Two major concerns with retrieving the pig were its weight (it could
weigh 6,000 lbs. wet) and the possibility of it becoming lodged in the
next outlet sump/pipe entrance and blocking flow (thus requiring the
flow to be turned off for retrieval). Because of the anticipated high
concentration of suspended solids, it was decided that the flow should
remain high for at least 48 hours in order to keep the solids in
suspension until the water reached the Lubbock reservoir. Jim Gammill of
Girard stated that the pig would not absorb so much water that it would
loose its buoyancy and that it would float when it fell out of the pipe
stand. Straps could then be lowered around the pig for removal by the
crane.
1st Pig Run
Launching/Retrieving
The first pig run went as anticipated except that the buoyant force on
the pipe beams was so great that the pig could not launch. The pipe had
to be drained enough so that the pig could be forced up to the pipe
opening allowing little water to pass. This proved to be sufficient as
the pig launched with approximately 10 to 15 feet of head.
With the use of the pig tracker, the pig was monitored to determine an
approximate arrival time and also to locate the pig in case it became
lodged. The pig averaged between 2.7 and 3.0 feet per second, roughly
85-90% of the velocity of the water. Approximately 10 minutes before the
pig arrived at Pipe Stand 3776+97.93, the water increasingly became more
turbid and eventually a brownish color. Also, several minutes ahead of
the pig, a thumping in the ground could be felt.
The pig came out of the riser pipe and fell over on top of the water
just as expected. Members of the crew lowered lifting straps around the
pig for easy removal of the pig by the crane.
C-Values
After the first run, water levels in the vent structures were measured
to determine if there was any noticeable change in the C-value. The most
recent measurements indicated that the C-value was approximately 111
before pigging. Immediately afterwards, measurements indicated that the
C-value had risen to 123 (an 11% increase). Measurements taken the next
day (March 27) also produced a C-value of 123. Figure 2 shows C-values
for the last 16 years for this section up the second pig run.

Figure 2 - C Values
Pig Inspection
The day following the first run the pig was inspected for damage and
wear. Surprisingly, a majority of the pig didn’t seem to have rubbed or
touched the pipe wall, as there was little wear on the polyurethane
coating or the wire brushes as can be seen in Figure 3. The fact that
the C-value had increased substantially and yet the pig showed limited
wear was somewhat puzzling. It was decided to run the pig a second time
to see if additional benefits could be accomplished.
2nd Pig Run
Pipe Inspection
When the line was drained in preparation for the second pig run, the
first 100-ft. of the pipe was inspected to see what effect the pig had
on the CaCO2 buildup. Surprisingly, there was little evidence
that the pig had smoothed the inner wall of the pipe much less remove
any buildup. The evidence didn’t seem to be consistent with the
increased C-value, as previously discussed.

Figure 3 - Pig Inspection After Being Run
Launching/Retrieving
Because of the problems with launching the first time, the pipe fork
used to prevent the pig from launching prematurely was not put in front
of the pig as the pipe was being filled with water. However, before the
water rose high enough to force the pig up against the pipe beams, the
pig was pulled up to the pipe opening by the flowing water. A few
minutes later, the pig launched with little head and with the pipe not
completely filled.
Because of the concern of surging, the flow was left at a low rate (6-10
cfs) to allow time for water to bypass the pig and fill the line ahead.
This put the pig moving at less than .5 fps. The progress of the pig was
monitored by watching the clarity of the water at the air valves. After
all or most of the air was removed from the line, the flow was increased
to 50 cfs and then 80 cfs for the last hour of the run.
There was some difficulty in retrieving the pig partly because of 40-mph
winds and light weight lifting straps that floated in the water.
C-Values
Once again, the C-value increased, however, not as much as after the
first run. The C-values increased from approximately 123 to 130 as shown
in Figure 2. Since a C-value of 130 is close to that of new concrete
pipe, it was decided to monitor this section and save the pig for
possible future runs. The pig project raised the C-value a total of 17%.
Water Analysis
Prior to the pig arrival on the second run, a water sample was taken so
that tests could be performed to determine the content of the suspended
solids. The results indicate that a high percentage (up to 95 %) of the
suspended solids is calcium carbonate. The sample was tested for organic
materials but no significant amount was found.
The central system (Pipe Stand 3044+16 to Pipe Stand 5107+02) is currently being pigged on an annual basis when other maintenance issues don't interfere.
| Lake Meredith | |
| Current Depth (11-19-2008) |
53.50 feet |
| Current Volume (11-19-2008) |
103,700 acre feet |
| Record High (April 1973) | 101.85 feet |
| Record Low (July 8, 2008) | 45.25 feet |
|
USGS Real-Time Lake Elevation (subtract 2813 feet from above link for lake depth) |
|
| Canadian River | |
| USGS Gauging Station North of Amarillo at US 287 | |
| NOAA Advanced Hydrologic Prediction Service at US 287 | |